10 Oct - 10 Dec 2012 - Part 1 - Back in the USA and the 2 weeks that turned out to be 2 months!

Nimue
Mon 10 Dec 2012 03:09
Joe Wysong kindly met us again at Dulles, Washington
airport to drive us back to Deltaville; a car journey which took nearly 4
hours, including a stop for supper! We were both absolutely exhausted when
we arrived, so Joe headed off for another 2 hour drive home and we both fell
into bed! We sometimes forget the distances between places in the
USA and the driving time to get to them, but many thanks again Joe, much
appreciated!
We woke up to blue skies and glorious sunshine, but to our
horror noticed something odd with Nimue’s teak decks. A lot of the
caulking (the black stuff in between the wood) had come out. In fact
Michael thought that the birds had been pecking away as it, as there were tiny
pieces of black rubber all over the deck! We did have some concerns
earlier in the year that some of the caulking appeared to be ‘melting’. We
also knew that our friend’s (David & Jenny), had a Contest 48 built in the
same year as Nimue (2000) and they had the same problem whilst crossing the
Pacific in 2006 and ended up having their decks re-caulked. Apparently
there was a problem with quality of certain batches of caulking in 2000 and
no-one seems to be accountable! With Nimue, now 12 years old, we knew we
wouldn’t have a ‘leg to stand on’, so decided to ‘bite the bullet’ and have them
re-caulked. To minimise the already expensive job, we agreed to take out
the existing caulking, which ended us both working on our knees for a 7 full
days digging it out (without damaging the teak). A good test for Michael’s
new hip and in fact, he felt that all the bending did it some good!
Anyway, it was a horrible job, as we came across black gluey/tarry mixtures and
‘hard as a rock’ stuff. Mitch, an excellent woodworker and craftsman
followed after us and started work routing deeper grooves into the existing
teak, which would increase the overall longevity of the decks. He would
then squeeze the new caulking into the grooves, leave it for a week to cure and
then trim off to give a smooth finish.
The exceptionally long hot summer had taken it’s toll on poor
Nimue and she was in need of some well deserved ‘TLC’.
![]() ![]() Zimmerman Marine boatyard on a quiet day
and where Nimue had spent the summer behind the white building
(mid-right)
![]() ![]() Michael stripping out the old caulking
from the decks and the new caulking; curing
![]() Mitch the woodworker, squeezing in some
more caulking into the decks
The one expense we had planned prior to arrival back in the
USA, was to have a new spray hood (or as the American’s say “Dodger”) and Bimini
made. Prior to our return to the UK, we met with Wendy of Wendy’s Custom
Yacht Canvas to discuss our requirements. We contacted Wendy on several
occasions from the UK, insisting the work had to be completed within a couple of
weeks of our return, as we were meeting some Canadian friends in Norfolk at the
beginning of November. In fact the first morning back, she had arranged for
herself and the stainless steel man “Bob” to meet us at Nimue at 0900hrs. All
credit to Wendy, she and Bob arrived on time and we confirmed the details.
Unfortunately, now that we had discovered the problem with the decks, it would
appear that Wendy would have all the time in the world to complete the work!
C’est La Vie!
We then came to turn the steering wheel; it wouldn’t
budge! The yard were ‘up to their necks’ in work, so Michael
with the help of, yours truly, managed to take out the gearbox and autohelm
motor. Another good test for Michael’s new hip! Fortunately,
Zimmerman's had been very good in allowing Michael to use their workshop, so he
was able dismantle and clean up the parts. It turned out the gearbox was
okay and was re-installed, but the bearings in the autohelm motor had seized.
With the aid of special machine tool, Michael was able to get the bearings out,
enabling us to take them to NAPA in Deltaville to order new ones.
These arrived the following day and were successfully re-installed!
![]() ![]() The gearbox (which was okay )
..................................................and the autohelm motor which
required new bearings
![]() ![]() Michael using the machine tool to take
out the autohelm motor bearings
![]() Now here lies a story behind the broken fence!
it was a quiet Saturday morning and Michael was in the workshop and I heard
police sirens getting louder and louder. The next thing I saw was a man
running across the yard and a police car chasing him. The man jumped over
the fence, but the police car just smashed through it! The man was
eventually apprehended and was charged for a number of theft & drug related
offences! It was just like watching cops and robbers on the
‘telly’
Whilst waiting for the decks to be completed, Michael took the
opportunity to replace the engine room bilge pump and engine fan. The gearbox
oil cooler (the one temporarily fixed on way north in April 2012) and the
exhaust (rubber) were replaced too, so Nimue was getting her much deserved
TLC. Not being an engineer, my contribution was to clean and paint the
engine room, which was hardly a ‘walk in the park’, knowing that the skipper
would pick up on the bits I missed, or spot drips of paint on the engine. In the
end we were both very pleased with our efforts and I suggested that it would be
a good idea to replace the wooden door panel to the engine room with a glass
panel, so everyone could admire our good work!
![]() ![]() The new exhaust rubber in pretty blue
and it fitted in place in the engine room!
![]() ![]() The water maker pump cleaned up and
re-fitted and the new hoses fitted to the new gearbox oil
cooler
We managed to antifoul (or as the American’s say “Bottom
Paint”) Nimue completely in one day, so that we were ready to be dropped back in
the water on the following Friday. The antifoul paint (or the lack of a
particular brand) is another saga, but I’ll leave that for another
day!
![]() Michael dressed up in all his finery, to
do some preparation work on Nimue’s hull prior to
antifouling
Then came ‘Sandy’ (see Sandy blog), so launch day was
understandably delayed.
Nimue was eventually dropped into the water on the following
Thursday, only to find the engine battery had died, although Michael was able to
jump start the engine. Then our usual inspection of the propeller shaft
seal and guess what, it was leaking (which meant another ‘lift out’ to replace
it)? As it wasn’t leaking too badly, we decided to leave Nimue in the
water, as we were expecting Heather & Jonas to join us for a holiday (our
friends from Calgary, who we spent time with during our Caribbean trip on their
yacht, Sea Otter). Once they left, we arranged a short haul lift out and
Michael was able to install the new shaft seal within a few hours.
Heather & Jonas arrived during one of the colder spells
and although we spent a lovely 10 days together, it was bitterly cold for the
majority of the time, which necessitated keeping Nimue warm with heaters and
electric fans on full blast! We thoroughly enjoyed our excursions to
the revolutionary and civil war sites and being enlightened by Jonas’s extensive
knowledge on every type of cannon we came across! (See separate
blogs).
![]() ![]() All set for launch day; hence smiles all
round!
![]() ![]() xxxx in charge of the travel lift and at
last moving her from her summer home to the water!
![]() All clean and ready to
go!
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